38AC to the rescue!!!
I suspected that it was at least one key, and the same one as you thought. Yesterday, I was out of energy and ideas though.
This morning, I tried your method, and it worked! As you said, I withdrew the keys, pushed them in as far as possible and rocked the wheels in opposite directions. I did this with one key at a time. The culprit was the side opposite the injector pump. The other key was OK.
I had some some metal roof flashing in the shop, .012" thick to make a shim for the crankshaft keyway bed. Reinstalled the key with the shim and started the engine. The knock was not eliminated, but very much reduced.......on the right track!
That is the same flywheel with an over-width keyway. On the old damaged crankshaft the shaft keyway was also over-width. I had corrected that 12 years ago with shims made of steel from a broken tape measure blade cut to the taper of the Gib key, then installed along the side of the keyways. That worked.
This new crankshaft actually has proper width keyways on both ends, the Gibs are a very nice fit into the keyways. That left the one flywheel with a .017+" wider keyway. When I installed the suggested shim under the key in question, I also carefully cut two shims tapered to the profile of the upper half of the key. With the crank and wheel positioned with keyways to the side, I was able to work the shims into the .017" between the upper half of the side of the key and the side of the wheel keyway. Tapped the key home and started the engine.
OH Joy! The knock is gone!!! Ran under load for an hour, and will do so again this afternoon. So far all is good.
I am now thinking that I will get a new set of keys and as a more permanent solution, try carbon-rod's solution of weld build-up at the side of a key, then machine for a proper fit. (
https://listerengine.com/smf/index.php?topic=6547.msg75154#msg75154 ) I will have to arrange a bit of work with a shop to mill this for me, but at this point, I have some time...........as long as the temporary side shimming works.
I am sure open to any other more permanent solutions.
I thought of maybe spraying the whole flywheel and shaft end with salt water and let it corrode into a solid mass...................well, maybe not.
So, at the very least, the source of the knock has been located and temporarily repaired. The previously mentioned shim repair (of 12 years ago held up nicely for all that time..
Thank you again Butch for keeping me on track. This is not the first time your seemingly small tips (gathered by long experience) have made a huge difference in keeping my off-grid power system operating. As well, your balancing method was easy and very effective. Wish I had known and done it 12 years ago!
Cheers
Hugh