Just discovered your saga of the flywheel and read it from end to end. Superb work in the finest DIY tradition. I'm sure eventual outcome will be a usuable machine. I still wonder sometimes about a rail car wheel. Keep up the good work!!!
Zeke
Thanx for the compliments!
The saga has continued while I have been silent here. I have installed a DIY interface adapter that fits into the cavity in the timing cover on the JD175A that previously held the oil filter `rock screen`. This has provided two 3/8 inch ports run to an external 10 micron spin-on hydraulic oil filter. I struggled with some leaks at first but now have everything under control. In the process though I suspect a particle of broken o-ring or RTV sealant made it`s way into the pressure passage to the rocker arm gallery and partially blocked the spray nozzle thus starving the rocker arms of oil spray. I destroyed one pressed in steel bushing and compromised the other and did slight wear damage to the hardened rocker shaft in one 9 hour run.. I need to order a new replacement shaft. I have restored oil flow, machined and installed yellow brass bushings on both rockers and they have survived the latest 40 hour continuous system test with flying colors.
Mobile Bob will be pleased to hear that I abandoned the use of locktite on the rocker set screws and just torqued down the lock nuts with a few hammer taps on the box end wrench.
Here is a picture of the new full flow oil filter system. Use the scroll bar at the bottom of this post to see the whole image.

I believe that carbon buildup on the piston is a possible cause of the perplexing vibration event that I witnessed. At the time this was after a 30 hour run with very low fuel throughput (0.3`ish litres per hour) and a rather cool exhaust temp in the neighborhood of just 210 F. I have since run the engine hard to clear it out, reconnected all the belts and large flywheel and run the plant at higher fuel input (0.55 litres per hour) resulting in an exhaust temp of 300 F for 40 hours continuous at 1700 RPM with absolutely no changes in operating behaviour or distress.
I have also determined that the considerable drag of spinning the AC Kohler head with no electrical connection is nearly identical to asking the DC head to make an additional 500 watts of electricity. When the plant has everything belted up (both gen heads and large flywheel) and run at just 500 watt DC load to yield low hourly fuel consumption numbers, the inclusion of the unused AC head in the active belt path bumps the hourly fuel consumption up by a factor near 1.6X. This is terrible.
At the same time I have also determined that the addition of the large flywheel in the active belt path adds an insignificant amount to the fuel consumption.
I am pleased to report that my DC head is indeed capable of acting as a starter motor from the very 48 volt battery bank that it will be connected to as charger! I can therefore unbelt the AC head and still enjoy electric start. It turns out that with the large flywheel and DC head belted to the engine I absolutely cannot hand crank start the engine and electric start is absolutely necessary.
In the true tradition of the best DIY, I am making progress!
